Accident Flight Design CTSW N775CT,
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ASN Wikibase Occurrence # 284376
 
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Date:Saturday 25 August 2007
Time:17:20 LT
Type:Silhouette image of generic FDCT model; specific model in this crash may look slightly different    
Flight Design CTSW
Owner/operator:Private
Registration: N775CT
MSN: 05-05-01
Total airframe hrs:459 hours
Engine model:Rotax 912 ULS
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:St. George, Utah -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Salinas Municipal Airport, CA (SNS/KSNS)
Destination airport:Saint George Municipal Airport, UT (SGU/KSGU)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot had just purchased the special light sport airplane and was flying it cross country to his home. He had received several hours of flight training and completed a flight review in the airplane the day before the accident. The accident flight was uneventful until about 20 miles from the destination, at which point the engine began to run rough. The pilot determined that the choke had "worked its way back about 3/4 of an inch." He "eased" the choke off and the engine roughness stopped. The engine lost complete power about 5 miles from the destination as the pilot entered the downwind leg for landing on runway 16. The pilot reported that he attempted to glide to the airport; however, the sink rate was excessive and he located a small clearing in the boulders on the bluff ahead and elected "to stall in vertically rather than to tumble over the rocks horizontally." He intentionally stalled the airplane at an altitude of 10 feet above ground. The airplane impacted the terrain, nosed over and came to rest inverted. The pilot added that he could have deployed the airplane's BRS parachute (a rocket deployed emergency parachute system), but "chose not to because we could have been blown over the dense population area, very near" to the accident site. Fuel was observed leaking from the wreckage the day after the accident. Initially during post-accident examination, the engine could not be rotated by hand. A broken snap ring was found jamming the gears in the propeller gearbox. According to the engine manufacturer's representative, it is common to find this snap ring broken in engines that have sustained impact damage. The snap ring was replaced and the engine was test run. The engine developed near 100 percent performance. The ignition system was checked and functioned normally. No discrepancies were noted that would have prevented normal engine operation and production of power. The reason for the loss of engine power could not be determined.

Probable Cause: The loss of engine power during approach for an undetermined reason. Contributing to the accident was the lack of suitable terrain for the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA07FA240
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB SEA07FA240

Revision history:

Date/timeContributorUpdates
30-Sep-2022 15:48 ASN Update Bot Added

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