Accident Cessna 207A N73463,
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ASN Wikibase Occurrence # 284415
 
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Date:Thursday 16 August 2007
Time:18:20 LT
Type:Silhouette image of generic C207 model; specific model in this crash may look slightly different    
Cessna 207A
Owner/operator:Wright Air Service
Registration: N73463
MSN: 20700593
Year of manufacture:1980
Total airframe hrs:11479 hours
Engine model:Teledyne Continental IO-550
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Fairbanks, Alaska -   United States of America
Phase: Unknown
Nature:Ferry/positioning
Departure airport:Squaw Lake, AK
Destination airport:Fairbanks International Airport, AK (FAI/PAFA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial air taxi pilot was returning to base on a cross country positioning flight when he noticed that the engine oil pressure gauge was registering zero. He stated that the rest of the engine gauges appeared normal, and he elected to continue the flight. About 45 minutes later, the engine seized, and the pilot made a forced landing on an oil service road, where the airplane collided with a ditch and received substantial damage. Postaccident inspection of the engine by company maintenance personnel and an FAA airworthiness inspector disclosed that the engine seized due to a lack of oil. No preimpact signs of oil leakage were discovered. The FAA inspector noted that the engine was a high time engine, and was nearly ready for an overhaul. He indicated that the pilot could have returned to his departure airport, or landed at several suitable sites en route with engine power after the low oil pressure reading, but that he elected to continue towards the operator's base.

Probable Cause: The loss of engine power in cruise flight due to a lack of sufficient oil. A factor contributing to the accident was the pilot's improper in-flight decision to continue the flight after noting a loss of oil pressure.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC07LA085
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB ANC07LA085

Revision history:

Date/timeContributorUpdates
30-Sep-2022 16:22 ASN Update Bot Added

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