Fuel exhaustion Accident Beechcraft 77 Skipper N1837Y,
ASN logo
ASN Wikibase Occurrence # 284469
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 8 August 2007
Time:15:50 LT
Type:Silhouette image of generic BE77 model; specific model in this crash may look slightly different    
Beechcraft 77 Skipper
Owner/operator:Private
Registration: N1837Y
MSN: WA-309
Engine model:Lycoming O-235
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Bloomington, Indiana -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Bloomington-Monroe County Airport, IN (BMG/KBMG)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane sustained substantial damage during a forced landing to a cornfield after takeoff. The pilot reported that soon after takeoff from runway 17, he noticed the fuel gauge indicated less fuel on board than he expected. He attempted to return to the airport and land on runway 35. About 1/2 mile from runway 35, the engine lost power. The pilot made a "Mayday" report and attempted a forced landing to the grass field adjacent to the airport. He reported that he saw a large roll of hay in his line of flight, so he executed a forced landing to a cornfield and the airplane subsequently nosed over. The inspection of the airplane revealed that the left fuel tank was empty and had blue stains around the drain. The right fuel tank had only a cup of fuel. Wing tank placards indicated the unusable fuel in each wing tank was .5 gallons. The electric fuel pump contained some residual fuel, but it was not full. No fuel was in the line between the carburetor and the fuel pump. The out line of the fuel pump contained a small amount of fuel. The carburetor bowl contained about 5 to 10 drops of fuel. No mechanical deficiencies were found that would have precluded normal engine operation. The pilot reported that he had flown the airplane about 10 days prior to the accident flight, and that he had calculated that there was about 2 hours of fuel remaining in the aircraft. He reported that on the day of the accident flight, he did not use a dipstick to check for the amount of fuel on board the airplane. He reported that he checked the fuel gauges and they indicated there was fuel on board. He reported that he was not sure if he had visually checked inside the fuel tanks.

Probable Cause: The loss of engine power due to fuel exhaustion as a result of the pilot's inadequate preflight.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI07CA262
Status: Investigation completed
Duration: 2 months
Download report: Final report

Sources:

NTSB CHI07CA262

Revision history:

Date/timeContributorUpdates
30-Sep-2022 17:13 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org