ASN Wikibase Occurrence # 284502
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 31 July 2007 |
Time: | 14:30 LT |
Type: | Cessna 185E |
Owner/operator: | Private |
Registration: | N70020 |
MSN: | 18501895 |
Total airframe hrs: | 3693 hours |
Engine model: | Continental IO-520-O24 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Talkeetna, Alaska -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | Stephan Lake, AK |
Destination airport: | Anchorage-Lake Hood, AK (LHD/PALH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The float-equipped airplane was being operated by the commercial pilot as a VFR cross-country flight in conjunction with his guiding service. The pilot said that he departed one lake en route to another, and about 20 minutes into the flight, the engine went to idle rpm. He said he pushed the throttle forward, and turned the airplane toward a lake, but the airplane descended into trees short of the lake. The airplane sustained extensive damage to the wings and fuselage. The pilot said that there were no known mechanical problems with the airplane prior to the flight. The airplane was examined, and it was found that the support shaft for the throttle and mixture bell cranks was missing, which disconnected the throttle control and allowed the engine to go to idle. The air induction box assembly was examined by the NTSB investigator, and it was discovered that the air box had been repaired with incorrectly substituted parts. The air box (PN 1650012-1) was the correct air box; however, a weld repair had been performed around the shaft support bushings on both sides of the box. The correct solid shaft bushings had been replaced with earlier generation roller bearings. The inappropriate installation did not allow for the support shaft to be properly pinned in place, and did not allow for the redundant safety of the correct installation. The correct parts installation would preclude the support shaft from migrating out of the air box if either shaft end spacer were missing. An examination of the airplane's maintenance log books did not reveal any entries pertaining to the air box repair.
Probable Cause: The loss of engine power during cruise flight due to an improperly repaired airbox.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC07LA071 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB ANC07LA071
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
30-Sep-2022 17:42 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation