Accident Cessna 185E N70020,
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ASN Wikibase Occurrence # 284502
 
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Date:Tuesday 31 July 2007
Time:14:30 LT
Type:Silhouette image of generic C185 model; specific model in this crash may look slightly different    
Cessna 185E
Owner/operator:Private
Registration: N70020
MSN: 18501895
Total airframe hrs:3693 hours
Engine model:Continental IO-520-O24
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Talkeetna, Alaska -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:Stephan Lake, AK
Destination airport:Anchorage-Lake Hood, AK (LHD/PALH)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The float-equipped airplane was being operated by the commercial pilot as a VFR cross-country flight in conjunction with his guiding service. The pilot said that he departed one lake en route to another, and about 20 minutes into the flight, the engine went to idle rpm. He said he pushed the throttle forward, and turned the airplane toward a lake, but the airplane descended into trees short of the lake. The airplane sustained extensive damage to the wings and fuselage. The pilot said that there were no known mechanical problems with the airplane prior to the flight. The airplane was examined, and it was found that the support shaft for the throttle and mixture bell cranks was missing, which disconnected the throttle control and allowed the engine to go to idle. The air induction box assembly was examined by the NTSB investigator, and it was discovered that the air box had been repaired with incorrectly substituted parts. The air box (PN 1650012-1) was the correct air box; however, a weld repair had been performed around the shaft support bushings on both sides of the box. The correct solid shaft bushings had been replaced with earlier generation roller bearings. The inappropriate installation did not allow for the support shaft to be properly pinned in place, and did not allow for the redundant safety of the correct installation. The correct parts installation would preclude the support shaft from migrating out of the air box if either shaft end spacer were missing. An examination of the airplane's maintenance log books did not reveal any entries pertaining to the air box repair.

Probable Cause: The loss of engine power during cruise flight due to an improperly repaired airbox.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC07LA071
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB ANC07LA071

History of this aircraft

Other occurrences involving this aircraft
6 June 1993 N70020 Private 0 Anchorage, AK sub

Revision history:

Date/timeContributorUpdates
30-Sep-2022 17:42 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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