Accident RotorWay Exec 162F N636PB,
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ASN Wikibase Occurrence # 284876
 
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Date:Monday 21 May 2007
Time:17:00 LT
Type:Silhouette image of generic EXEC model; specific model in this crash may look slightly different    
RotorWay Exec 162F
Owner/operator:Private
Registration: N636PB
MSN: 6636
Total airframe hrs:17 hours
Engine model:Rotorway 150W
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Argyle, New York -   United States of America
Phase: Unknown
Nature:Training
Departure airport:Private strip, NY
Destination airport:ARGYLE, NY (NY02)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The certified flight instructor (CFI) stated that the purpose of the flight was instruction. He conducted a preflight of the helicopter and did not note any problems with the helicopter. Start up and run up was completed by the checklist with no problems. They lifted off, hovered for a few minutes and landed again. Shortly thereafter they departed an airport for training. The takeoff and climb were normal, and they leveled off at 1,500 feet. Approximately 3 miles from the airport, the engine began to run rough and there was a drop in power. The dual student transferred the flight controls to the CFI. The CFI decided not to continue the flight to the airport, and initiated an approach to a field behind a house. On approach the engine stopped, and an autorotation was initiated to the field. The touchdown was "smooth" and level, with a slow forward speed. The helicopter slid approximately 10 feet and rolled over onto the left side. Examination of the helicopter by an FAA inspector revealed no flight control anomalies. The pilot reported that the helicopter was fine until the engine power began decrease. The examination of the engine revealed that the number 4 rocker arm was unsecured and the spring retainer was damaged. Further examination revealed that the number 4 exhaust valve had stuck in the open position. In a review of the logbook it was discovered that the mechanic had made valve lash adjustments to all the cylinders on September 16, 2006, at an engine tachometer time of 17.4 hours. The engine tachometer time at the accident site was 18.1 hours. The engine had .7 hours before the exhaust valve failed. The cylinder heads were sent to Rotorway International for examination of the exhaust and intake valves. According to Rotorway, examination of the heads revealed that the exhaust valves were found to be "sticky in their guides". The guide size measured at the low side of the tolerance before cleaning. After cleaning with a wire brush, the fit of the valves in the cylinder heads and the tolerance of sizes were acceptable.

Probable Cause: The loss of engine power due to the sticking of the exhaust valves that resulted from carbon buildup.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL07CA084
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB ATL07CA084

Revision history:

Date/timeContributorUpdates
01-Oct-2022 09:56 ASN Update Bot Added

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