ASN Wikibase Occurrence # 284995
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Date: | Thursday 26 April 2007 |
Time: | 14:15 LT |
Type: | Cessna 150L |
Owner/operator: | Private |
Registration: | N1557Q |
MSN: | 15072857 |
Year of manufacture: | 1971 |
Total airframe hrs: | 5860 hours |
Engine model: | Continental O-200 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Watsonville, California -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Watsonville Airport, CA (WVI/KWVI) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane nosed over in a wheat field following a loss of engine power during takeoff. The certified flight instructor (CFI) estimated that 10 to 15 minutes elapsed between completion of the run-up and takeoff checklist before traffic cleared so that he and the student could take off. The takeoff was normal, and they started their climb to the practice area. About 200 to 300 feet agl, the engine started to lose power; it didn't just lose power. He took control. He applied carburetor heat, and pumped the throttle a few times as he had done in the past to keep an engine running. However, the engine didn't respond. The airplane was over the end of the runway. He felt that they were too low to turn around, and wanted to get the airplane down before they flew past the clear area before a freeway. He aimed for a wheat field that he thought would cushion the landing. He estimated that about 40 seconds elapsed from the loss of power to touchdown. The wheat in the field was 4-feet tall, and a lot thicker than the CFI expected. It stopped the airplane on touchdown, causing a nose over. He saw fire in the engine compartment. He instructed the student to be careful unstrapping since they were inverted, but to hurry. They both exited out the right side door, and cleared the airplane. The FAA coordinator examined the airplane and engine and no abnormalities were found to preclude normal operation.
Probable Cause: a partial loss of engine power for undertermined reasons during takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX07CA135 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB LAX07CA135
Revision history:
Date/time | Contributor | Updates |
01-Oct-2022 16:19 |
ASN Update Bot |
Added |
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