ASN Wikibase Occurrence # 285203
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Date: | Saturday 3 March 2007 |
Time: | 07:45 LT |
Type: | Mooney M20D |
Owner/operator: | |
Registration: | N6628U |
MSN: | 123 |
Year of manufacture: | 1963 |
Total airframe hrs: | 3664 hours |
Engine model: | Lycoming O-360-A1D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Visalia, California -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Concord-Buchanan Field, CA (CCR/KCCR) |
Destination airport: | Visalia Airport, CA (VIS/KVIS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane collided with a berm during a forced landing in an industrial building construction site following a loss of engine power. The pilot stated that during the preflight inspection he did not check the fuel quantity. He stated that a month prior to the accident the airplane had been "topped off," and then flown about an hour from the right fuel tank. The pilot also said that during the 160 nautical mile accident flight he did not recall switching fuel tanks. About 3 miles north of the destination airport the engine sputtered and lost power. He switched tanks and activated the electric fuel boost pump, the engine restarted momentarily, then sputtered and lost power again. The pilot switched tanks three or four more times to no avail. Post accident inspection of the airplane by the FAA revealed that the right fuel tank was empty and the left tank contained about 6 gallons of 100LL aviation fuel. The fuel line to the carburetor did not contain any fuel. The fuel selector valve was selected to the right tank position. The electric fuel pump was activated and no fuel pressure indication was observed. The fuel selector handle was moved to the left fuel tank position and a fuel pressure indication was observed in the normal operating range.
Probable Cause: The pilot's inadequate in-flight fuel system management, which resulted in fuel starvation and a loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX07CA098 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB LAX07CA098
History of this aircraft
Other occurrences involving this aircraft
29 May 2009 |
N6628U |
Private |
1 |
Near Clintwood, Virginia |
|
sub |
Revision history:
Date/time | Contributor | Updates |
01-Oct-2022 19:15 |
ASN Update Bot |
Added |
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