ASN Wikibase Occurrence # 285204
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Date: | Friday 2 March 2007 |
Time: | 18:35 LT |
Type: | Cessna 150G |
Owner/operator: | Dean International, Inc. |
Registration: | N682RA |
MSN: | 15067007 |
Year of manufacture: | 1967 |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Miami, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Homestead, FL (X51) |
Destination airport: | Miami Executive Airport, FL (TMB/KTMB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The certified flight instructor (CFI) stated that the engine began to run rough while performing airwork during an instructional flight. He elected to divert to a nearby airport where he performed an uneventful precautionary landing. While on the ground he performed an engine run-up and noticed a discrepancy with the left magneto. He operated the engine to a high rpm setting with the fuel/air ratio leaned in an effort to clear what he thought was lead fouled spark plugs, and reported that the left magneto drop was within limits (150 rpm). The CFI did not contact the operator to get assistance related to the precautionary landing, and elected to return to the original departure airport. During climbout, when the flight was 6-7 miles from the destination airport, the engine vibrations began and the rpm fluctuated 200 rpm, decreased to 2,000 rpm, then further decreased and remained at 300-400 rpm. He maneuvered the airplane towards a grass airstrip that he knew about, but because of the low light and visibility restriction, he flew past the airstrip. Due to the low altitude, he elected to land in a field perpendicular to the airstrip. While approaching the field, the airplane collided with powerlines then the ground, and nosed over. Postaccident examination of the engine revealed no evidence of a failure or malfunction of the power section. Examination of the fuel system revealed no evidence of preimpact failure or malfunction. Examination of the spark plugs were satisfactory but were wet with oil consistent with an inverted engine. The left magneto operated intermittently during postaccident bench testing. Disassembly of the left magneto revealed the point cam was worn, and the points exhibited erosion. Additionally, the coil tested out of limits; the condenser tested within specification.
Probable Cause: The pilot-in-command's (CFI) continued operation of the airplane with known deficiencies (rough running engine). A factor in the accident was no suitable terrain for a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA07LA055 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB MIA07LA055
Revision history:
Date/time | Contributor | Updates |
01-Oct-2022 19:15 |
ASN Update Bot |
Added |
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