Accident Hughes 369D N1088G,
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ASN Wikibase Occurrence # 285363
 
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Date:Thursday 4 January 2007
Time:13:10 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 369D
Owner/operator:Highline Helicopters
Registration: N1088G
MSN: 700736D
Year of manufacture:1980
Total airframe hrs:5504 hours
Engine model:Allison 250/C20B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Lyman, Washington -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:Lyman, WA
Destination airport:Lyman, WA
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot made two long-line movements of cargo in light dry snow. After completing the second load, the pilot noticed that the snow had turned wet and heavy, and he told the ground crew that he was leaving the area. As he turned to depart the area, one of the ground crew radioed him and said that he was going to pass near one of the loads, and suggested that he pick it up. The pilot maneuvered toward the load, and entered into a hover to swing the long-line hook forward. Just as he entered the hover, the engine lost power, and the pilot delayed his emergency autorotation to allow the ground crew person to find cover. Because the rotor system energy decayed during the pilot's intentional delay of the autorotation, he was unable to control the descent, and the helicopter settled onto the terrain at an excessive rate of descent. The pilot stated that when he changed the angle of attack to put the hook in the right location, he believes a layer of wet snow and ice crystals lifted off the canopy and entered the engine particle separator, leading to a loss of engine power. A postaccident inspection did not reveal evidence of any system malfunction or anomaly.

Probable Cause: The pilot's intentional flight into adverse weather conditions, which resulted in a loss of engine power during hover due to snow and ice ingestion. Factors associated with the accident are the pilot's delayed remedial actions, and snow and icing conditions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA07LA041
Status: Investigation completed
Duration: 3 months
Download report: Final report

Sources:

NTSB SEA07LA041

History of this aircraft

Other occurrences involving this aircraft
9 June 1994 N1088G Highline Helicopters 0 Snoqualmie, WA sub
18 March 2024 N102SU Signature Utility Services, LLC 0 near Belleville, WV sub
Energy sector

Revision history:

Date/timeContributorUpdates
02-Oct-2022 08:41 ASN Update Bot Added

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