ASN Wikibase Occurrence # 285535
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Date: | Saturday 4 October 2008 |
Time: | 10:30 LT |
Type: | Cessna T210M |
Owner/operator: | Private |
Registration: | N11PC |
MSN: | 21062600 |
Year of manufacture: | 1978 |
Total airframe hrs: | 3825 hours |
Engine model: | Continental TSIO-520 SER |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Savannah, Georgia -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | Trenton-Mercer County Airport, NJ (TTN/KTTN) |
Destination airport: | Brunswick-Malcolm McKinnon Airport, GA (SSI/KSSI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was fueled twice in an effort to obtain maximum fuel capacity, then secured in a hangar and was not operated; no fuel leakage was noted on the hangar floor. The pilot did not visually inspect the fuel tanks during her preflight inspection, contrary to the Pilot's Operating Handbook. The flight departed with an inoperative right fuel quantity gauge and proceeded towards the destination airport with fuel supplied from both fuel tanks at different times and durations. Approximately 3 hours and 35 minutes into the flight, while the left fuel tank was supplying fuel, the engine experienced a momentary surge that stopped when the pilot reduced throttle control. At that time the left fuel quantity gauge indicated approximately 35 minutes of fuel remaining at normal cruise power; however, the pilot thought it should have 24 gallons remaining and attributed the error to be an indicator problem. The flight continued and she positioned the fuel selector to the right tank and flew for a few minutes, then repositioned the fuel selector to the left tank, for which the fuel quantity gauge indicated zero. Several minutes later the engine lost power due to fuel exhaustion. She notified air traffic control and was vectored to the nearest airport but was unable to land there. She ditched the airplane in a marsh, and was rescued by the U.S. Coast Guard. No unusual fuel flow was reported to have occurred during the accident flight. Postaccident inspection of the wreckage revealed no fuel in either fuel tank or in fuel lines in the engine compartment. No fuel leak was noted and there was no evidence of engine preimpact failure or malfunction.
Probable Cause: A loss of engine power in flight due to fuel exhaustion as a result of the pilot's improper fuel management.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09LA004 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB ERA09LA004
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 11:09 |
ASN Update Bot |
Added |
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