ASN Wikibase Occurrence # 285622
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Date: | Wednesday 3 September 2008 |
Time: | 11:57 LT |
Type: | Sadler Vampire |
Owner/operator: | Sadler Aircraft |
Registration: | N333SV |
MSN: | 054 |
Total airframe hrs: | 52 hours |
Engine model: | Rotamex 1300CG |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Findlay, Ohio -
United States of America
|
Phase: | Initial climb |
Nature: | Test |
Departure airport: | Findlay Airport, OH (FDY/KFDY) |
Destination airport: | Findlay Airport, OH (FDY/KFDY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was an experimental amateur-built airplane that was a prototype for light sport aircraft certification. The flight test was conducted by the engine manufacturer, who also provided a pilot to fly the airplane. The pilot had not received flight instruction or a checkout in the airplane. The pilot learned to fly the airplane on his own by taxiing and performing local flights in the airport area. The pilot also had no training or experience in aircraft flight test. A larger radiator had been installed onto the airplane due to noted high engine temperature during previous flights. Prior to the accident flight, the pilot performed two taxi tests during which he performed short hops on the runway to get familiar with the aerodynamic forces that would be encountered during takeoff and landing. The engine temperature was reported as normal during this time. The pilot then attempted a takeoff for a flight that was to remain in the airport traffic pattern. Just after takeoff the airplane lost total engine power. The pilot attempted an engine restart without success, during which he did not hear the engine turn over. The pilot then executed a forced landing into a quarry located about 0.6 miles from the departure end of the runway. An examination of the reduction drive assembly needle roller bearing sidewall revealed a combination of wear and high temperatures leading to overstress. Circumferential wear marks on the separated cage sidewall and the presence of metallic debris suggested impingement of the rollers on the sidewall during engine operation. Heat tinting of the outer raceway in the vicinity of the failed sidewall and the cam that served as the inner raceway was also noted. The needle bearing malfunction could be attributed to misalignment of the needle bearing and insufficient lubrication.
Probable Cause: A total loss of engine power due to the failure of the reduction drive assembly as a result of excessive wear and high temperatures. Contributing to the accident were the pilot's lack of total experience in the airplane and the unsuitable terrain for a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI08LA274 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB CHI08LA274
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 12:28 |
ASN Update Bot |
Added |
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