ASN Wikibase Occurrence # 285681
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 19 August 2008 |
Time: | 09:20 LT |
Type: | Cessna TU206F |
Owner/operator: | Airwest Helicopters LLC |
Registration: | N62DB |
MSN: | U206 03278 |
Total airframe hrs: | 6301 hours |
Engine model: | Teledyne Continental TSIO-520-C |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Glendale, Arizona -
United States of America
|
Phase: | Standing |
Nature: | Unknown |
Departure airport: | Glendale Municipal Airport, AZ (KGEU) |
Destination airport: | Valle, AZ (40G) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the engine began to run rough shortly after takeoff. Unable to return to the airport, he initiated a forced landing in a short field. The airplane collided with a fence during the landing roll. During a post crash examination, a loose fuel line fitting was discovered that was connected to the fuel flow transducer inlet. It was also noted that there were blue stains on the crankcase immediately below the fitting. After tightening the fitting, the engine started and ran smoothly at 1,800 revolutions per minute (rpm) with a smooth rpm drop for each magneto. The fitting was then manually loosened again with the engine running at 1,800 rpm, the fuel pressure fell below the bottom of the green arc, and the engine began to run rough. The fitting was again tightened, and smooth engine operation resumed. The last maintenance recorded that would have involved removal of this fitting was during an engine replacement on July 7, 2007, which was 127 hours prior to the accident.
Probable Cause: A loose fuel line fitting that resulted in a partial loss of engine power during the initial takeoff climb. Contributing to the accident was inadequate maintenance installation of the fitting.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX08LA269 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX08LA269
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 13:19 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation