ASN Wikibase Occurrence # 285829
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Date: | Monday 21 July 2008 |
Time: | 11:30 LT |
Type: | Grumman G-164D Turbo Ag-Cat |
Owner/operator: | Erickson Aerial Spraying LLC |
Registration: | N996QC |
MSN: | 19C |
Year of manufacture: | 1978 |
Engine model: | Pratt & Whitney PT6A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Esmond, North Dakota -
United States of America
|
Phase: | Initial climb |
Nature: | Agricultural |
Departure airport: | Esmond, ND (KPVT) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he gradually added power during takeoff to minimize the prop wash which tended to suck the hopper door open allowing the chemical load to spray out of the hopper and onto the windshield. The pilot reported the airplane became airborne in ground effect with one-third of the runway distance remaining. The airplane settled back onto the airstrip and became airborne once again with 300 to 500 feet of runway remaining. The pilot began to dump the chemical load when he reached the end of the airstrip; however, the airplane began to settle toward the ground again. The left spray boom contacted a wheat crop and the airplane cartwheeled into the field. The pilot purchased the airplane approximately 3 weeks prior to the accident. He stated the hopper door seal was leaking so he had the seal replaced and the door clamps adjusted. He stated he realized the door needed extra clamps on its forward and aft ends to keep it from opening. He stated he had one clamp which they put on the aft end of the door because it would not fit on the forward end. The pilot had an additional clamp on order for the forward end. The pilot stated he did not dump the load earlier because he did not want to kill the grass on the airstrip.
Probable Cause: The pilot's delay in advancing the throttle during the takeoff which resulted in inadequate airspeed and the subsequent stall/mush. Factors associated with the accident were the leaking hopper, the pilot continuing to operate the airplane with the known deficiency, and the pilot's delay in dumping the chemical load.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI08CA201 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI08CA201
History of this aircraft
Other occurrences involving this aircraft
23 May 2012 |
N996QC |
Private |
0 |
Northeast of Sedgwick, AR |
|
sub |
Mid-air collision |
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 15:39 |
ASN Update Bot |
Added |
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