Loss of control Accident Grumman G-164D Turbo Ag-Cat N996QC,
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ASN Wikibase Occurrence # 285829
 
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Date:Monday 21 July 2008
Time:11:30 LT
Type:Silhouette image of generic G64T model; specific model in this crash may look slightly different    
Grumman G-164D Turbo Ag-Cat
Owner/operator:Erickson Aerial Spraying LLC
Registration: N996QC
MSN: 19C
Year of manufacture:1978
Engine model:Pratt & Whitney PT6A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Esmond, North Dakota -   United States of America
Phase: Initial climb
Nature:Agricultural
Departure airport:Esmond, ND (KPVT)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he gradually added power during takeoff to minimize the prop wash which tended to suck the hopper door open allowing the chemical load to spray out of the hopper and onto the windshield. The pilot reported the airplane became airborne in ground effect with one-third of the runway distance remaining. The airplane settled back onto the airstrip and became airborne once again with 300 to 500 feet of runway remaining. The pilot began to dump the chemical load when he reached the end of the airstrip; however, the airplane began to settle toward the ground again. The left spray boom contacted a wheat crop and the airplane cartwheeled into the field. The pilot purchased the airplane approximately 3 weeks prior to the accident. He stated the hopper door seal was leaking so he had the seal replaced and the door clamps adjusted. He stated he realized the door needed extra clamps on its forward and aft ends to keep it from opening. He stated he had one clamp which they put on the aft end of the door because it would not fit on the forward end. The pilot had an additional clamp on order for the forward end. The pilot stated he did not dump the load earlier because he did not want to kill the grass on the airstrip.

Probable Cause: The pilot's delay in advancing the throttle during the takeoff which resulted in inadequate airspeed and the subsequent stall/mush. Factors associated with the accident were the leaking hopper, the pilot continuing to operate the airplane with the known deficiency, and the pilot's delay in dumping the chemical load.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI08CA201
Status: Investigation completed
Duration: 2 months
Download report: Final report

Sources:

NTSB CHI08CA201

History of this aircraft

Other occurrences involving this aircraft
23 May 2012 N996QC Private 0 Northeast of Sedgwick, AR sub
Mid-air collision

Location

Revision history:

Date/timeContributorUpdates
02-Oct-2022 15:39 ASN Update Bot Added

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