ASN Wikibase Occurrence # 285839
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Date: | Friday 18 July 2008 |
Time: | 21:30 LT |
Type: | Piper PA-28-161 |
Owner/operator: | Private |
Registration: | N2133V |
MSN: | 28-7916323 |
Year of manufacture: | 1979 |
Total airframe hrs: | 7167 hours |
Engine model: | Lycoming O-320-036 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sparta, Wisconsin -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Sparta Fort Mc Coy Airport, WI (KCMY) |
Destination airport: | Madison-Dane County Regional Airport, WI (MSN/KMSN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he had landed at the airport to refuel, and the accident occured during an aborted takeoff when it departed the end of the 4,708-foot by 100 feet, asphalt runway. He reported that he "filled the tanks to 28 gallons total via visual inspection." After another preflight that included "sumping" the fuel tanks, he conducted a full power engine run with the brakes held at the threshold of runway 29. He reported that the engine was performing normally during full power ground roll as the airplane's airspeed increased. He reported, "Entering ground effect in order to achieve airspeed for safe climb performance I observed only partial power." He lowered the nose and applied brakes; however, the airplane went off the end of runway 29 at about 15 mph. The pilot reported that the terrain sloped downward about 15 degrees and the grass was wet with dew. He was unable to stop the airplane before the landing gear collapsed and the wing spar was bent. The engine was test run after the accident, and it produced 2,375 RPM. The total weight of the airplane at the accident site was about 2,486 pounds. The maximum gross weight limit of the airplane was 2,440 pounds.
Probable Cause: The pilot's inadequate preflight planning and the pilot's delay in aborting the takeoff. Contributing to the accident was the airplane's overgross weight condition.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI08LA197 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB CHI08LA197
Location
Revision history:
Date/time | Contributor | Updates |
02-Oct-2022 15:50 |
ASN Update Bot |
Added |
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