Accident Rockwell 690B Turbo Commander N9KG,
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ASN Wikibase Occurrence # 285926
 
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Date:Wednesday 25 June 2008
Time:15:00 LT
Type:Silhouette image of generic AC90 model; specific model in this crash may look slightly different    
Rockwell 690B Turbo Commander
Owner/operator:Private
Registration: N9KG
MSN: 11426
Year of manufacture:1977
Total airframe hrs:5509 hours
Engine model:Garrett TPE-331-10T
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Baker City, Oregon -   United States of America
Phase: Landing
Nature:Private
Departure airport:Portland-Hillsboro Airport, OR (HIO/KHIO)
Destination airport:Baker Airport, OR (BKE/KBKE)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane sustained substantial damage following a right main landing gear collapse on its first landing after a 150-hour maintenance inspection. The collapse was due to a fracture and separation of the right main landing gear's housing boss from the inboard hydraulic cylinder clevis. The 150-hour inspection included the installation of a new clevis on the right main landing gear's inboard hydraulic actuator. A postaccident examination by a Federal Aviation Administration inspector revealed that the inboard hydraulic rod bearing attach bolt was screwed all the way in, which was contrary to instructions specified in the maintenance manual. While the manual states that the attach bolt should be backed off three complete turns in order to maintain proper rigging, the manufacturer reported that improper preload adjustment of the right main landing gear actuator cylinder could not create a large enough force to induce the failure of the right main landing gear outer body boss and clevis fitting. A metallurgical examination of the inboard hydraulic cylinder clevis and associated clevis pin housing boss showed that the housing boss had fractured from the main body of the strut and that the fracture was consistent with overstress. There was no evidence of wear or fatigue cracking on either the clevis or the housing boss. The postaccident examination of the airplane, the landing gear system, and its associated components failed to reveal the initiating event that subsequently resulted in the overstress failure and landing gear collapse.

Probable Cause: The landing gear collapse during the landing roll due to the fracture of the inboard hydraulic cylinder clevis pin housing boss for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA08LA157
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:

NTSB SEA08LA157

History of this aircraft

Other occurrences involving this aircraft
16 August 2021 C-GYLD MAG Aerospace Canada Corp. 1 Thunder Bay Airport (YQT/CYQT), ON w/o
Loss of control

Location

Revision history:

Date/timeContributorUpdates
02-Oct-2022 17:10 ASN Update Bot Added

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