Hard landing Accident Cessna 152 N49811,
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ASN Wikibase Occurrence # 286326
 
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Date:Friday 1 February 2008
Time:08:30 LT
Type:Silhouette image of generic C152 model; specific model in this crash may look slightly different    
Cessna 152
Owner/operator:West Valley Flying Club
Registration: N49811
MSN: 15281332
Year of manufacture:1978
Total airframe hrs:6730 hours
Engine model:Lycoming O-235-L2C
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Palo Alto, California -   United States of America
Phase: Standing
Nature:Ferry/positioning
Departure airport:Palo Alto Airport, CA (PAO/KPAO)
Destination airport:San Carlos Airport, CA (SQL/KSQL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Prior to the accident flight, a maintenance inspection was performed. A piece of the baffling was found in the throat of the carburetor venturi. The carburetor was inspected and reinstalled on the airplane. On the accident flight, the pilot/mechanic performed a post maintenance run-up with no mechanical problems noted. She taxied the airplane to the runway for takeoff and performed another run-up. Again there were no mechanical problems noted, and all the gages showed normal indications. On the takeoff roll the engine developed 2,300 rpm's. About 500 feet mean sea level (msl), she noticed a hesitation in the engine and decided to make a 180-degree turn back to the runway. The airplane was still high on the approach, so the pilot reduced the airspeed, performed S-turns, and then slipped the airplane to lose altitude. She was still high, and about halfway down the runway, she further reduced the airspeed, which increased the sink rate. She lowered the nose to slow the sink rate, and was in the process of raising the nose again to flare for landing when the nose struck the runway. An inspection of the engine revealed zero compression of the number 1 cylinder with blow-by past the piston rings and exhaust valve. Maintenance personnel also noted that the bottom number 1 cylinder spark plug was "excessively" fouled with carbon deposits. There were no problems noted with the carburetor.

Probable Cause: Loss of engine power during the takeoff initial climb due to lack of compression to a cylinder.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX08LA055
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB LAX08LA055

Location

Revision history:

Date/timeContributorUpdates
03-Oct-2022 09:01 ASN Update Bot Added

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