ASN Wikibase Occurrence # 287052
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Date: | Thursday 16 April 2009 |
Time: | 09:15 LT |
Type: | Cessna 152 |
Owner/operator: | Sunrise Aviation |
Registration: | N64988 |
MSN: | 15281515 |
Total airframe hrs: | 7286 hours |
Engine model: | Lycoming O-235 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Cross City, Florida -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Cross City Airport, FL (CTY/KCTY) |
Destination airport: | Ormond Beach Municipal Airport, FL (KOMN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While climbing through 3,400 feet mean seal level (msl), the newly certificated private pilot noticed that the engine power decreased by approximately 300 rpm; however, the engine was running smoothly with no abnormal noise. The pilot verified that the engine controls were in the proper position and he then positioned the carburetor heat to "ON." The engine power continued a steady decay to 1,400 rpm as the airplane descended to 1,000 feet msl and the pilot elected to perform a forced landing to a field that he had been circling. During the landing, he overshot his intended touchdown point. The airplane subsequently struck two fence posts and came to rest inverted in the field. Review of fueling records revealed that the airplane had adequate fuel to complete the round trip cross-country flight. The engine crankshaft and carburetor were damaged during impact, which limited the field examination of those components. The cabin heat was noted in the "ON" position and the carburetor heat was in the "OFF" position; however, the carburetor box had been pulled from the airframe during impact. Examination of the wreckage could not identify the reason for the engine power loss. Review of a Federal Aviation Administration Carburetor Icing Chart revealed "Serious icing - glide power" for the reported temperature and dew point conditions.
Probable Cause: Loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09LA247 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB ERA09LA247
History of this aircraft
Other occurrences involving this aircraft
22 July 1993 |
N64988 |
Free Spirit Aviation, Inc. |
0 |
Howell, MI |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
03-Oct-2022 19:55 |
ASN Update Bot |
Added |
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