ASN Wikibase Occurrence # 287068
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Date: | Thursday 9 April 2009 |
Time: | 10:45 LT |
Type: | Byron J. Moore Zealot |
Owner/operator: | Private |
Registration: | N61ZT |
MSN: | 061 |
Total airframe hrs: | 200 hours |
Engine model: | Rotax 582 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Clermont, Florida -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | Mascotte, FL (06FD) |
Destination airport: | Mascotte, FL (06FD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that he was in cruise flight at 1,800 feet when the motorized glider experienced a total loss of engine power. He attempted an engine restart with negative results and made a forced landing. The current owner stated that he purchased the motor glider about 4 months before the accident. The engine had been removed by the previous owner, rebuilt, serviced, installed on the glider, and placed in storage. A Federal Aviation Administration inspector disassembled the engine after the accident. Prior to disassembly, the oil tank indicated that it was full of oil. Disassembly of the engine revealed the rotary valve disc drive gear had failed due to insufficient lubrication. There were about 2 ounces of oil drained from the oil bath reservoir. The engine manufacturer's installation manual indicated that if the vent plug in the engine case is not removed when servicing the engine with oil. The oil reservoir can indicate it is full of oil, and an air bubble can form which will prevent oil from filling the chamber. This will result in significant heat, and cause catastrophic failure of the drive gear due to insufficient lubrication. The previous owner stated that he did not remove the vent plug when he serviced the oil after the engine was rebuilt and installed on the motor glider.
Probable Cause: A loss of engine power due to oil starvation as a result of the previous owner's improper servicing of the engine oil.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09LA238 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA09LA238
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 06:59 |
ASN Update Bot |
Added |
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