ASN Wikibase Occurrence # 28717
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Date: | Wednesday 16 January 2008 |
Time: | 12:15 |
Type: | Cessna 207 Skywagon |
Owner/operator: | Inland Aviation Services Inc. |
Registration: | N1701U |
MSN: | 20700301 |
Year of manufacture: | 1975 |
Total airframe hrs: | 18448 hours |
Engine model: | Continental IO-520 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Aniak, AK -
United States of America
|
Phase: | Approach |
Nature: | Ferry/positioning |
Departure airport: | Crooked Creek, AK (CJX) |
Destination airport: | Aniak, AK (PANI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial certificated pilot was returning from a remote village after a round robin flight of about 130 miles over a frozen and snow-covered river. He was in cruise flight about 500 feet agl, but then circled while holding between 6 or 7 miles east of his destination airport, awaiting a special VFR (SVFR) clearance. The weather condition in that area was about 1 mile visibility, with a ceiling of about 1,000 feet agl. After receiving his SVFR clearance, the pilot flew toward the airport, but the engine fuel pressure began fluctuating. The engine rpm began decreasing, along with the airplane's altitude. The pilot switched fuel tanks, selected full flaps, and prepared for a forced landing. He said the weather was near white-out conditions, but he could see the bank of the river. After switching fuel tanks from the left to the right tank, the engine power suddenly returned to full power. He applied forward flight control pressure to prevent the airplane from climbing too fast, but the airplane collided with the surface of the river. The airplane sustained structural damage to the wings and fuselage. At the time of the accident, the ceiling at the airport was 600 feet obscured, with a visibility of 1/2 mile in snow. Neither the fuel status of the accident airplane, nor the mechanical condition of the engine, were verified by either the NTSB or FAA.
Probable Cause: A partial loss of engine power for an undetermined reason. Contributing to the accident were the pilot's inadvertent encounter with IMC conditions, and a whiteout during his attempted go-around from an emergency landing approach.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC08LA032 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
20700301
Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
21-Aug-2011 13:32 |
TB |
Updated [Date, Time, Aircraft type, Registration, Cn, Operator, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
23-Feb-2017 17:19 |
TB |
Updated [Source, Narrative] |
03-Dec-2017 09:25 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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