ASN Wikibase Occurrence # 287447
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Date: | Friday 24 August 2012 |
Time: | 08:26 LT |
Type: | Cessna 152 |
Owner/operator: | Sunrise Aviation Inc |
Registration: | N24264 |
MSN: | 15280183 |
Year of manufacture: | 1977 |
Total airframe hrs: | 9345 hours |
Engine model: | Lycoming O-235 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ormond Beach, Florida -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Ormond Beach Municipal Airport, FL (KOMN) |
Destination airport: | Gainesville-J R Alison Municipal Airport, FL (GNV/KGNV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot took off in calm wind conditions, and, although he reported that pretakeoff checks were normal, he did not believe that the airplane was climbing properly after liftoff. Air traffic control tower personnel observed the airplane lift off and touch down twice before running off the end of the runway. The airplane came to rest about 625 feet beyond the end of the runway. The pilot recognized a loss of airplane performance during the initial takeoff and successfully landed the airplane back on the runway. However, instead of stopping the airplane, the pilot took off again, which then put the airplane in a position where a second aborted takeoff could only result in a runway overrun. Postaccident examination revealed no preexisting mechanical anomalies that would have precluded normal operations, and flight instructors who flew the airplane during its two previous flights noted no discrepancies during those flights. The ambient temperature and dew point about the time of the accident indicated a probability of carburetor ice accumulation during taxi, and the carburetor heat was found in the off position.
Probable Cause: The pilot's improper decision to take off again after a successful abort due to diminished airplane climb performance. Contributing to the accident was carburetor icing during the taxi, which resulted in the loss of engine performance.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA525 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB ERA12LA525
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 10:58 |
ASN Update Bot |
Added |
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