ASN Wikibase Occurrence # 287451
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Date: | Wednesday 22 August 2012 |
Time: | 11:50 LT |
Type: | Grumman American AA-1B |
Owner/operator: | |
Registration: | N9858L |
MSN: | AA1B-0458 |
Year of manufacture: | 1974 |
Total airframe hrs: | 3940 hours |
Engine model: | Lycoming 0-235-C2C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bedford, Pennsylvania -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Fort Meade/Odenton-Tipton AAF, MD (FME/KFME) |
Destination airport: | Bedford County Airport, PA (KHMZ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that the airplane began to porpoise after landing. When his efforts to correct the porpoise and continue the landing were not successful, the pilot decided to go around. During the attempted go-around, the pilot did not believe that he was going to clear some trees and decided to land the airplane in a field. The nose and right main landing gear collapsed after touchdown, resulting in substantial damage to the fuselage and both wings. The pilot stated that there were no preaccident mechanical issues and that the engine was producing full power. However, he added that the airplane's engine only produced 100 horsepower and that he did not feel as though he was gaining enough altitude and was 'behind the airplane†during the go-around. Examination of the airplane revealed that carburetor heat control was "ON," the throttle was in the full open position, and the mixture control was in the full rich position. Review of the airplane's owner's manual revealed that the pilot should immediately apply full power and turn the carburetor heat off during a go-around. Further review of the owner's manual indicated that, based on the airplane's basic empty weight, the weights of the occupants, and the fuel on board, the airplane was operating at or near its published maximum gross weight during the accident.
Probable Cause: The pilot's failure to maintain control of the airplane during the landing and subsequent go-around. Contributing to the accident was the pilot's failure to shutoff the carburetor heat during the attempted go-around and the weight at which the airplane was being operated.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12CA523 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB ERA12CA523
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 10:59 |
ASN Update Bot |
Added |
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