ASN Wikibase Occurrence # 287597
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Date: | Monday 9 July 2012 |
Time: | 09:25 LT |
Type: | Beechcraft A36 |
Owner/operator: | Aircraft Engineering Inc |
Registration: | N6672B |
MSN: | E-1584 |
Year of manufacture: | 1979 |
Total airframe hrs: | 3776 hours |
Engine model: | Continental IO 550-B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Johns Island, South Carolina -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Bartow Airport, FL (BOW/KBOW) |
Destination airport: | Charleston Executive Airport, SC (KJZI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was in cruise flight when it experienced symptoms of an electrical failure and the alternator "fail" light illuminated. A normal deployment of the landing gear was unsuccessful, so the pilot had the non-pilot-rated passenger review the manual gear extension procedure and then attempt to lower the gear. The pilot "confirmed" the landing gear handle would no longer rotate, but the electrical power loss precluded confirmation by the landing gear lights. The airplane completed a "no-bounce" landing and then settled to the runway on its belly, which resulted in substantial damage to airframe stringers and frames; the damage was consistent with the landing gear doors being closed during landing. According to a mechanic who supervised the recovery of the airplane from the runway, the airplane was resting on its belly with the landing gear retracted. He said the gear was "maybe 5 percent" deployed but remained retracted as the airplane was lifted with straps. Another mechanic entered the airplane, engaged the manual gear handle, and lowered the gear to the down and locked position. The battery master switch was turned on, and three green down-and-locked lights illuminated.
Probable Cause: The pilot's failure to complete the manual emergency gear extension after a loss of electrical power. Contributing to the accident was the pilot's decision to delegate the landing gear extension to a non-pilot-rated passenger.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA450 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB ERA12LA450
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 12:30 |
ASN Update Bot |
Added |
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