ASN Wikibase Occurrence # 287803
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Date: | Monday 9 April 2012 |
Time: | 12:30 LT |
Type: | Air Tractor AT-602 |
Owner/operator: | Boyle Flying Service Inc |
Registration: | N51037 |
MSN: | 602-0464 |
Year of manufacture: | 1997 |
Total airframe hrs: | 5311 hours |
Engine model: | P&W Canada PT6A-66 SER |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ruleville, Mississippi -
United States of America
|
Phase: | Standing |
Nature: | Agricultural |
Departure airport: | Boyle, MS |
Destination airport: | Boyle, MS |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on an aerial application flight with an estimated 53 gallons of fuel. He had not reset the fuel totalizer before departure. He made numerous passes over a 100-acre field spraying fertilizer during the 30 minute flight. After his last pass, the pilot noticed a fuel flow fluctuation. The engine subsequently lost power at an altitude of 75 to 100 feet above the ground, and the pilot made a forced landing. He pulled the airplane off the ground again briefly to clear an obstruction; however, when the airplane touched down again, the left main landing gear sank into soft ground and sheared off. The airplane rotated to the right onto its nose, and the left wing sustained structural damage. Postaccident examination revealed that the left and right main fuel caps had a tight seal and there was no evidence of streaking or venting of fuel on the airplane or on the ground. The left, right, header, and purge fuel tanks were drained and yielded about 34 total ounces of fuel—two ounces from the right fuel tank and 32 ounces from the header tank. The left and purge tanks contained no fuel. No preaccident mechanical malfunctions or failures were found that would have precluded normal operation.
Probable Cause: The pilot's inadequate preflight planning and in-flight fuel management, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12CA275 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB ERA12CA275
History of this aircraft
Other occurrences involving this aircraft
9 April 2010 |
N51037 |
Boyle Flying Service, Inc |
0 |
Ruleville, MS |
|
sub |
4 June 2021 |
N51037 |
Boyle Flying Service Inc |
0 |
Drew, Mississippi |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 14:36 |
ASN Update Bot |
Added |
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