ASN Wikibase Occurrence # 287990
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 14 October 2010 |
Time: | 10:40 LT |
Type: | Mischke BD-5B |
Owner/operator: | David Mischke |
Registration: | N525BD |
MSN: | 2 |
Total airframe hrs: | 119 hours |
Engine model: | Yamaha Nytro |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Burlington, Washington -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Mount Vernon-Skagit Regional Airport, WA (MVW/KBVS) |
Destination airport: | Mount Vernon-Skagit Regional Airport, WA (MVW/KBVS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that shortly after takeoff for the local area flight the engine's rpms decreased and he felt a loss of thrust. The pilot made a turn in an attempt to make an emergency landing to another runway; however, the airplane touched down hard and short of the runway, substantially damaging the airplane. Postaccident examination revealed that the sprag clutch failed, preventing the engine from turning the propeller and causing a loss of thrust.
Probable Cause: The failure of the sprag clutch during takeoff, resulting in a loss of engine thrust.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR11LA015 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB WPR11LA015
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 17:30 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation