ASN Wikibase Occurrence # 288029
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Date: | Tuesday 28 September 2010 |
Time: | 12:20 LT |
Type: | Cessna 310R |
Owner/operator: | Baker George |
Registration: | N455TB |
MSN: | 310R1860 |
Total airframe hrs: | 3561 hours |
Engine model: | Continental TSIO-520 SER |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Great Falls, Montana -
United States of America
|
Phase: | Taxi |
Nature: | Private |
Departure airport: | Lethbridge Airport, AB (YQL/CYQL) |
Destination airport: | Great Falls International Airport, MT (GTF/KGTF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While on approach to his planned destination, the pilot lowered the landing gear handle, but the green "gear down" light for the right main landing gear did not illuminate, and the "gear in transition" light stayed on. After checking the "gear down" light, which illuminated when pushed, the pilot reached the conclusion that the problem was most likely a bad gear position indicator switch, which was a problem he had experienced before. The pilot then considered cycling the landing gear, but decided not to do so in case there was something broken in the system that might result in the right main gear remaining up once it was retracted. He then executed an uneventful landing and rollout, which included slowing to his normal taxi speed. At that point he turned off the runway onto the taxiway, and as he began to straighten the airplane to follow the taxiway centerline, the right main gear to folded back, causing the right wing to impacted the taxiway. A postaccident inspection determined that the right main gear upper side link (over-center lock) had not moved fully to its locked position, and that the side-loads generated by the turn to align with the taxiway were transferred to the gear activation system. The transfer of those loads then resulted in the overload failure of the right main gear strut-mounted bellcrank. It could not be determined what caused the right main landing gear activation linkage to be far enough out of adjustment as to result in the upper side link not moving to its fully locked position.
Probable Cause: The uncommanded retraction of the right main landing gear during taxi due to the failure of the landing gear extension system to move the right main gear upper side link into the locked position for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA476 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB WPR10LA476
History of this aircraft
Other occurrences involving this aircraft
26 June 2016 |
N455TB |
Smith Loren |
0 |
Schafer Meadows, Montana |
|
sub |
Runway excursion |
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 17:49 |
ASN Update Bot |
Added |
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