ASN Wikibase Occurrence # 288060
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Date: | Saturday 18 September 2010 |
Time: | 16:15 LT |
Type: | Beechcraft 58 Baron |
Owner/operator: | Albatross Aircraft Sales Inc |
Registration: | N86BR |
MSN: | TH-1072 |
Year of manufacture: | 1979 |
Total airframe hrs: | 5321 hours |
Engine model: | Continental IO 550 C |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Rainelle, West Virginia -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Morgantown Airport, WV (MGW/KMGW) |
Destination airport: | Bluefield-Mercer County Airport, WV (BLF/KBLF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, while in cruise flight, the right engine lost power. He attempted to move the left fuel selector to the crossfeed position in an attempt to restart the right engine, but the fuel selector knob would not turn clockwise to that position. Shortly thereafter, the left engine lost power. The pilot feathered both propellers and set the airplane up for its best glide angle in an attempt to reach the closest airport. His attempts to restart the engines during the descent were unsucessful. The pilot made a forced landing in the backyard of a private residence, and the airplane collided with a house, sustaining substantial damage. A postaccident examination of the fuel system revealed that the fuel selectors were indicating "on" for both fuel tanks, and the left fuel selector knob would not rotate clockwise to the crossfeed position. When the left fuel selector valve was disassembled, it was found to be rigged incorrectly. In the 'on†position, the valve should have drawn fuel from the left and right fuel tanks. Instead, it drew fuel from the right tank only. The right fuel tank was found to be empty of all usable fuel. A review of the airplane's maintenance records revealed that the left fuel selector was removed, resealed, and reinstalled prior to the accident.
Probable Cause: The improper rigging of the fuel selector by maintenance personnel, which resulted in a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA10LA485 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB ERA10LA485
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 18:08 |
ASN Update Bot |
Added |
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