ASN Wikibase Occurrence # 288160
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Date: | Monday 23 August 2010 |
Time: | 16:15 LT |
Type: | Cessna 182A Skylane |
Owner/operator: | William Burr |
Registration: | N3850D |
MSN: | 34550 |
Year of manufacture: | 1957 |
Total airframe hrs: | 5877 hours |
Engine model: | Teledyne Continental O-470 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ojai, California -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Sacramento-McClellan Airfield, CA (MCC/KMCC) |
Destination airport: | Santa Paula, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was on the return leg of a cross-country flight and the pilot added about 16 gallons of fuel before departure. During the flight, he noticed that the alternator-out light was illuminated, and the voltmeter indicated a discharge, but this would not have affected the already-running engine. The airplane was in cruise flight at 7,500 feet mean sea level when it suddenly lost engine power; the pilot said that the power did not decrease gradually or sputter. The pilot indicated that he tried numerous methods to restart the engine without success. The direct-sight fuel gauges were indicating between the 1/4 and 1/3 levels. The airplane was losing altitude, and the pilot decided to try to land on a golf course. He left the flaps in the up position to extend his glide. During the final stage of the descent, the right wing hit a tree. After touchdown, the airplane hit a bush and spun around before coming to a stop. Examination of the wreckage revealed no evidence of preimpact mechanical malfunction of the airframe or engine that would have precluded normal operation. The environmental conditions were not conducive to carburetor icing.
Probable Cause: A loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10FA423 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB WPR10FA423
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 19:09 |
ASN Update Bot |
Added |
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