ASN Wikibase Occurrence # 288282
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Date: | Sunday 25 July 2010 |
Time: | 13:30 LT |
Type: | Air Tractor AT-602 |
Owner/operator: | Har-mor Ag Air Inc |
Registration: | N8521L |
MSN: | 602-0703 |
Year of manufacture: | 2004 |
Total airframe hrs: | 1745 hours |
Engine model: | Pratt & Whitney Canada PT6A-60A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Yates City, Illinois -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | Monmouth, IL (C66) |
Destination airport: | Monmouth, IL (C66) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that after he completed the aerial application, he climbed to 500 to 600 feet above ground level. After he leveled the airplane, he heard a loud sound and the engine lost power. He executed a forced landing to a cornfield, during which the wings and fuselage sustained substantial damage. The pilot reported that he had about 50 to 75 gallons of fuel remaining in the wing tanks, when the accident occurred. The postaccident inspection of the airplane revealed that no fuel was visible in the left and right wing tanks, but fuel was observed coming out of the right wing root. The engine was removed from the airframe and fuel was found in the fuel lines and fuel filter. The postaccident inspection of the airframe, engine, and engine components revealed no preimpact anomalies that would preclude normal engine operation. According to the lineman who fueled the airplane prior to departure, the right tank was full, and the left tank was nearly full. The endurance for the airplane was 3.2 hours; it had been flying for about 1 1/2 hours when the loss of power occurred.
Probable Cause: The loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN10LA437 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB CEN10LA437
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 20:50 |
ASN Update Bot |
Added |
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