ASN Wikibase Occurrence # 288434
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 16 June 2010 |
Time: | 12:15 LT |
Type: | Aeronca 7AC |
Owner/operator: | John S Stoll |
Registration: | N84362 |
MSN: | 7AC-3057 |
Total airframe hrs: | 2337 hours |
Engine model: | Continental O-200 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sandersville, Georgia -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Moncks Corner-Berkeley County Airport, SC (KMKS) |
Destination airport: | Macon-Lewis B. Wilson Airport, GA (MCN/KMCN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on the cross country flight with a full load of fuel. As he began a descent to enter the traffic pattern at the destination airport, the pilot reduced engine power to 1,500 rpm and applied carburetor heat. The engine began losing power, so the pilot removed carburetor heat and applied throttle; but the engine then lost power completely. The pilot unsuccessfully attempted to restore engine power, and subsequently performed a forced landing. The airplane impacted a berm approximately 1/4 mile from the runway threshold, which resulted in substantial damage. A postacccident examination revealed that the fuel header tank contained approximately 8.5 gallons of uncontaminated fuel. During subsequent testing, the engine started, ran continuously, and showed no evidence of any mechanical anomalies. While the airplane was operating in conditions conducive to serious carburetor icing at glide power at the time of the accident, the investigation was unable to determine if carburetor ice caused the power loss.
Probable Cause: A total loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA10LA314 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA10LA314
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2022 22:39 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation