Accident Piper PA-32R N6911Z,
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ASN Wikibase Occurrence # 288512
 
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Date:Tuesday 18 May 2010
Time:08:00 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R
Owner/operator:
Registration: N6911Z
MSN: 32R-8529015
Year of manufacture:1985
Total airframe hrs:4083 hours
Engine model:Lycoming TIO540-S1AD
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Alpine, Texas -   United States of America
Phase: Take off
Nature:Private
Departure airport:Alpine, TX (E38)
Destination airport:Fort Stockton-Pecos County Airport, TX (FST/KFST)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he performed an engine run-up prior to departure and everything was normal. He then advanced the throttle, prop control, and mixture from left to right and monitored the ehxhaust gas temperature (EGT) to make sure the temperature stayed in the high 1300-degree to low 1400-degree range during the takeoff roll. However, on this takeoff roll he noted that the EGT was reading 1450 degrees so he increased mixture to lower the temperature. Everything seemed to normalize until he became airborne and the engine spooled back. The pilot noted that the EGT was still high at 1440 degrees, so he attempted to land on the remaining stretch of runway. There was not enough room and the airplane exited the runway and collided with a deer fence. Examination of the engine revealed that the flexible hose and two clamps that connect the intercooler to the turbocharger inlet were not installed properly, which caused the flexible hose to slide out of position. The engine had been overhauled in 2007 and installed back on the airplane using the same propeller and accessories. There were no entries between the time the engine was installed to the date of the accident that indicated that either the turbocharger or the intercooler had been worked on. The last annual inspection was performed exactly one year prior to the accident.

Probable Cause: improper installation of the flexible hose and two clamps that connect the intercooler to the turbocharger.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN10LA259
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB CEN10LA259

Location

Revision history:

Date/timeContributorUpdates
04-Oct-2022 23:28 ASN Update Bot Added

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