ASN Wikibase Occurrence # 288721
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 8 February 2010 |
Time: | 11:50 LT |
Type: | Aerocomp Comp Air 7SL |
Owner/operator: | |
Registration: | N286JL |
MSN: | 057222 |
Total airframe hrs: | 100 hours |
Engine model: | Walter 601D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Merritt Island, Florida -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Tallahassee International Airport, FL (TLH/KTLH) |
Destination airport: | Cocoa-Merritt Island Airport, FL (COI/KCOI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot of the experimental, amateur-built, turboprop airplane, the airplane was configured for landing while on the downwind and base legs for runway 29. During the final approach segment, the airplane was aligned with the runway centerline and airspeed and power were stabilized. At the approach end of the runway, the airplane suddenly dropped, resulting in a hard bounce. Corrections were made and on the second bounce, power was added for a go-around procedure. The engine did not respond to the thrust lever input. The continued bouncing resulted in a loss of directional control and the airplane exited the runway to the left. According to the owner/pilot-rated-passenger, the pilot turned downwind and at base leg, was exceeding the recommended approach speed by 20 knots. Upon turn to final they were approaching the runway 'hot.†Airspeed was 80 plus knots and the stall speed for the airplane was 68 to 70 knots. The airplane bounced hard and a go-around was attempted, but was unsuccessful because the turbine spooling was too slow. The airplane exited the runway to the center median with another hard bounce, then with the ensuing crash. The pilot reported that she had accumulated a total time of 15,000 hours; of which, 3.5 hours were in the accident airplane.
Probable Cause: The pilot's failure to maintain control of the airplane during landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA10CA145 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB ERA10CA145
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 01:32 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation