ASN Wikibase Occurrence # 289463
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Date: | Saturday 19 March 2011 |
Time: | 14:15 LT |
Type: | Piper PA-18A 150 |
Owner/operator: | Van Wagner Aerial Media LLC |
Registration: | N9692D |
MSN: | 18-6800 |
Year of manufacture: | 1959 |
Total airframe hrs: | 14678 hours |
Engine model: | Lycoming O-360-C2A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hollywood, Florida -
United States of America
|
Phase: | Initial climb |
Nature: | Banner and glider towing |
Departure airport: | Hollywood-North Perry Airport, FL (HWO/KHWO) |
Destination airport: | Hollywood-North Perry Airport, FL (HWO/KHWO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on a banner tow flight with an adequate supply of fuel, and flew for about 1.5 hours before returning to the departure airport. He dropped the first banner, descended, then climbed to pick up the second banner. As he applied power, the engine initially responded, but then it lost power about 50 to 100 feet above ground level with no sputtering noted. The pilot applied forward elevator control input and verified that the mixture was full rich and that the fuel selector was on the left tank. Prior to touchdown, he applied aft elevator control input, but there was no response, and the airplane landed hard. Operator personnel reported that both magneto switches were in the on position, the fuel selector was in the left tank position, the carburetor heat was pulled slightly, the throttle was full forward, and the mixture control was slightly leaned.
Postaccident examination of the airplane revealed that the inboard and outboard fuel tanks contained fuel; however, the amount in each tank was not quantified. However, the amount was adequate to sustain engine power. No fuel was found in the fuel strainer; however, fuel was in the carburetor bowl. A replacement propeller was installed, and the engine was test run and it operated satisfactorily. The conditions about the time of the accident were favorable for serious carburetor icing at glide power. The reason for the lack of fuel in the fuel strainer and the loss of engine power could not be determined.
Probable Cause: A total loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA11LA200 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB ERA11LA200
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 14:06 |
ASN Update Bot |
Added |
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