Gear-up landing Accident Mooney M20R N1034S,
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ASN Wikibase Occurrence # 289839
 
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Date:Sunday 4 August 2013
Time:11:10 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20R
Owner/operator:Red's Flying Service Inc
Registration: N1034S
MSN: 29-0456
Year of manufacture:2006
Total airframe hrs:373 hours
Engine model:Continental IO-550-G
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Tallahassee, Florida -   United States of America
Phase: En route
Nature:Private
Departure airport:Tallahassee International Airport, FL (TLH/KTLH)
Destination airport:Bartow Airport, FL (BOW/KBOW)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Shortly after departing on an instrument flight rules flight, the airplane abruptly lost all electrical power while operating in instrument meteorological conditions. The pilot reported that, given the abrupt nature of the electrical power loss, he assumed that it was due to a short circuit; he did not troubleshoot the electrical problem. He then descended the airplane to visual meteorological conditions and used a portable electronic device to navigate back toward the departure airport. During the return flight, the pilot was concerned about a possible electrical fire and smoke in the cockpit and wanted to land the airplane as soon as possible; therefore, he chose not to perform the emergency procedure to manually extend the airplane's electrically actuated landing gear. Upon reaching the airport, he conducted a gear-up landing, which resulted in substantial damage to the fuselage.

Postaccident examination of the airplane's electrical system found that the No. 2 battery was inoperable and that the total loss of electrical power was likely caused by an internal electrical short of the battery. When the electrical system's redundant (No. 1) battery was selected, the electrical system operated normally. It is likely that, if the pilot had attempted to troubleshoot or isolate the electrical problem, he could have restored electrical power, extended the landing gear normally, and executed a precautionary landing without damaging the airplane. Alternatively, he could have manually extended the landing gear.

Probable Cause: The pilot's failure to troubleshoot the in-flight electrical problem and restore power using the operable redundant battery and his decision not to manually extend the airplane's landing gear, which resulted in a gear-up landing. Contributing to the accident was an internal electrical short of the No. 2 battery, which resulted in a total loss of electrical power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA13LA363
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB ERA13LA363

Location

Revision history:

Date/timeContributorUpdates
05-Oct-2022 18:48 ASN Update Bot Added

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