ASN Wikibase Occurrence # 289864
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Date: | Saturday 27 July 2013 |
Time: | 09:22 LT |
Type: | Piper PA-28-181 |
Owner/operator: | |
Registration: | N371JB |
MSN: | 28-8490106 |
Year of manufacture: | 1984 |
Total airframe hrs: | 6900 hours |
Engine model: | Lycoming O&VO-360 SER |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Columbus, Georgia -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Columbus-Metropolitan Area, GA (CSG/KCSG) |
Destination airport: | Columbus-Metropolitan Area, GA (CSG/KCSG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Another pilot reported that she had aborted a takeoff on a previous flight in the accident airplane when she felt that the engine was not developing sufficient power. The accident pilot subsequently arrived at the airport, they "checked everything again," and he attempted to take off. However, both pilots again "felt the same thing," and the accident pilot aborted that takeoff attempt. The accident pilot subsequently attempted to take off again, but, after feeling that the engine was not developing enough power, he decided to land straight ahead. During the landing, the airplane bounced once and overran the runway end; it then pivoted 180 degrees before coming to a stop. The accident pilot also indicated that he and the other pilot originally thought that there was an airspeed indication problem. The accident pilot looked at the pitot head after his first aborted takeoff and noticed debris, which he removed. He then performed a high-speed taxi test to ensure that the airspeed indicator was functioning properly before the final takeoff attempt. The airplane was sold for parts before it could be further examined for possible performance-related anomalies.
Probable Cause: The pilot's delayed decision to abort the takeoff. Contributing to the accident was the airplane's perceived lack of performance for reasons that could not be determined due to insufficient information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA13LA337 |
Status: | Investigation completed |
Duration: | 1 year and 11 months |
Download report: | Final report |
|
Sources:
NTSB ERA13LA337
Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2022 19:06 |
ASN Update Bot |
Added |
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