ASN Wikibase Occurrence # 290192
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 15 February 2013 |
Time: | 15:00 LT |
Type: | Ayres S2R-T34 |
Owner/operator: | Coates Flying Service Inc |
Registration: | N3095X |
MSN: | T34-174 |
Year of manufacture: | 1991 |
Total airframe hrs: | 7190 hours |
Engine model: | P&W Canada PT6A-60A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Gaines, Georgia -
United States of America
|
Phase: | En route |
Nature: | Agricultural |
Departure airport: | Fort Gaines, GA (79GA) |
Destination airport: | Fort Gaines, GA (79GA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the airplane was topped off with 60 gallons of fuel prior to departure and that he applied a spray application to a field for about 30 minutes before returning to the airplane's home base. While enroute, the engine lost power and the pilot was unable to restart the engine. He then performed a forced landing in a field, during which both wings sustained substantial damage.
After the accident, about 35 gallons of fuel remained in the left wing and 5 gallons remained in the right wing. Postaccident examination indicated that the left forward wing fuel line was partially blocked; the aft left and both right wing fuel lines were free of obstruction. Additionally, the fuel control unit was contaminated with debris. All other fuel system parts were free of obstructions. The left forward fuel line and fuel fitting were sent to the NTSB materials laboratory for examination and were found to be blocked with debris consistent with soil. The debris in the left forward wing fuel line alone would not have reduced fuel flow to the engine; however, the contamination of the fuel control unit likely would have reduced fuel flow sufficient to cause fuel starvation. The investigation was unable to determine the origin of the debris.
Probable Cause: The total loss of engine power due to fuel starvation as a result of debris in the fuel control unit.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA13LA138 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB ERA13LA138
History of this aircraft
Other occurrences involving this aircraft
17 August 1996 |
N3095X |
Riddell Flying Service, Inc. |
0 |
W. Helena, AR |
|
w/o |
Location
Revision history:
Date/time | Contributor | Updates |
06-Oct-2022 11:56 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation