Runway excursion Accident Van's RV-6A N214MJ,
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ASN Wikibase Occurrence # 290423
 
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Date:Sunday 10 August 2014
Time:11:23 LT
Type:Silhouette image of generic RV6 model; specific model in this crash may look slightly different    
Van's RV-6A
Owner/operator:
Registration: N214MJ
MSN: 23212
Year of manufacture:1998
Total airframe hrs:1765 hours
Engine model:Aero Sport Power IO-360-M1
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:West Palm Beach, Florida -   United States of America
Phase: En route
Nature:Private
Departure airport:Kissimmee Gateway Airport, FL (ISM/KISM)
Destination airport:Pembroke Pines, FL (HWO
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, about 20 minutes into the flight and at 5,500 feet above mean sea level, the engine began "missing" but continued to run. This occurred about every minute and lasted about 1 second each time. He reported the engine issue to air traffic control, climbed the airplane to 10,000 feet, and eventually elected to divert to an airport about 13 miles away. He set up for an approach to land to the west; however, he crossed the runway threshold about 25 feet above the ground and at 110 knots. Unable to slow the airplane to a safe landing speed, he attempted a go-around. The engine "appeared to rev up" but he observed little power being produced. He discontinued the go-around and landed straight ahead. The airplane overran the runway at the departure end, and the pilot applied rudder and aileron controls to avoid striking a perimeter fence. The airplane flipped over and came to rest inverted, with substantial damage to both wings and extensive damage to the fuselage. The airplane was equipped with an electronic flight information system; however, it did not record any useful data. The airplane's fuel tanks appeared to contain an adequate amount of fuel for the flight. The engine was examined and no anomalies or failures were observed. The reason for the partial loss of engine power could not be determined after a full examination of the wreckage.

Probable Cause: The pilot's excessive landing speed, which resulted in a runway excursion and noseover. Contributing to the accident was a partial loss of engine power during an attempted go-around for reasons that could not be determined because no anomalies were identified during postaccident examination.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA14LA382
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB ERA14LA382

Location

Revision history:

Date/timeContributorUpdates
06-Oct-2022 14:59 ASN Update Bot Added

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