Runway excursion Accident de Havilland Canada DHC-2 Beaver N62197,
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ASN Wikibase Occurrence # 290450
 
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Date:Wednesday 30 July 2014
Time:22:30 LT
Type:Silhouette image of generic DHC2 model; specific model in this crash may look slightly different    
de Havilland Canada DHC-2 Beaver
Owner/operator:Glenn Air Inc.
Registration: N62197
MSN: 1177
Year of manufacture:1957
Total airframe hrs:12466 hours
Engine model:P & W R-985-AN-14B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Talkeetna, Alaska -   United States of America
Phase: Standing
Nature:Executive
Departure airport:Talkeetna, AK
Destination airport:Wasilla, AK (IYS)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane had been outfitted with a large, bulk fuel tank to transport fuel to remote sites. After a fuel delivery, the airplane departed from a soft, wet, and muddy sod-covered airstrip that was 1,400 ft long and 50 ft wide with a slight downhill grade. The pilot reported that, during the takeoff run, the airplane failed to become airborne before reaching the end of the airstrip, so he aborted the takeoff. The airplane overran the airstrip and sustained substantial damage to the wings and fuselage.

The operator stated that, before the fuel delivery, the airplane was loaded with about 180 gallons of aviation fuel and that, after arriving at the airstrip, the pilot got out of the airplane, connected a hose and transfer pump system to the bulk fuel tank, and operated the transfer pump for about 5 minutes. Postaccident examination of the wreckage revealed that all 180 gallons of fuel were still in the bulk fuel tank. According to the operator, the pilot did not open the drain valve to allow the tank to drain nor did he verify that the tank was empty before departing. Further, the operator stated that the pilot departed about midfield using only the last 750 ft of airstrip that remained; the estimated takeoff distance for the flight was between 800 and 900 ft.

Probable Cause: The pilot's inadequate preflight inspection that did not detect that the bulk fuel tank was full and led to an unanticipated heavy airplane weight and his failure to use the entire soft, wet, and muddy airstrip length for takeoff, which resulted in a takeoff overrun.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC14LA058
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB ANC14LA058

Location

Revision history:

Date/timeContributorUpdates
06-Oct-2022 15:17 ASN Update Bot Added

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