ASN Wikibase Occurrence # 290882
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 1 August 2015 |
Time: | 13:40 LT |
Type: | Air Tractor AT 502B |
Owner/operator: | C |
Registration: | N502LH |
MSN: | 502B-2693 |
Year of manufacture: | 2009 |
Total airframe hrs: | 2254 hours |
Engine model: | Pratt & Whitney PT6A-34A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Virden, Illinois -
United States of America
|
Phase: | Take off |
Nature: | Agricultural |
Departure airport: | VIRDEN, IL (25IL) |
Destination airport: | VIRDEN, IL (25IL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the airplane had just been loaded and that he was beginning his sixth agricultural application flight of the day. He noted that, during the previous flights, the wind was from the southwest-southeast and less than 5 knots. Before departing on the sixth flight, he checked the wind sock, which indicated that the wind was from the southwest. He also checked his handheld GPS, which indicated that the local area wind was mainly from the west at 3 to 5 knots. The pilot started the takeoff roll on the runway heading west and noted that, three-quarters of the way down the runway, the airspeed had not yet reached takeoff speed. He jettisoned some of the load so that the airplane could clear the corn at the end of the runway. When the airplane cleared the corn, the pilot ceased the jettison. However, the airplane then began to descend, so the pilot jettisoned more of the load. The airplane continued to descend, banked hard left, and impacted the ground.
The pilot reported that there were no mechanical malfunctions with the airplane that would have precluded normal operation. The airplane was only about 30 lbs below its maximum gross weight. Witnesses stated that, immediately after the accident, the wind was from the southeast about 6 knots, which would have resulted in a quartering tailwind during the takeoff. It is likely that the combined effects of the airplane's near maximum gross weight and the quartering tailwind degraded the airplane's climb performance during takeoff.
Probable Cause: The pilot's failure to establish a proper airspeed during takeoff with the airplane near its maximum gross weight and with a quartering tailwind.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA335 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB CEN15LA335
Location
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 06:49 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation