Accident Commander 114B N6566D,
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ASN Wikibase Occurrence # 290883
 
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Date:Saturday 1 August 2015
Time:13:19 LT
Type:Silhouette image of generic AC11 model; specific model in this crash may look slightly different    
Commander 114B
Owner/operator:Precision Machine Tool Solutions LLC
Registration: N6566D
MSN: 14671
Year of manufacture:2000
Total airframe hrs:1091 hours
Engine model:Lycoming IO-540-T4B5
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Reading, Pennsylvania -   United States of America
Phase: Standing
Nature:Private
Departure airport:Reading Regional Airport/Spaatz Field, PA (RDG/KRDG)
Destination airport:Reading Regional Airport/Spaatz Field, PA (RDG/KRDG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the airline transport pilot, about 30 minutes into the personal flight and while the airplane was at 3,000 ft mean sea level, the engine "seemed to lose power for a second." About 1 second later, the engine "shut off completely." The pilot tried to restart the engine by turning on the electric fuel boost pump and then moving the fuel selector to each of the positions without success. He then moved the fuel selector back to the "both tanks" position and set the nose pitch for best glide speed; however, the airplane was unable to glide to the airport, so the pilot set it up for an off-field landing. During the forced landing, the airplane encountered uneven terrain, and the right wing struck a tree.

A postaccident engine test run was conducted, and the engine would not start. Subsequent examination of the engine revealed that a fuel supply line fitting at the fuel manifold was loose and that fuel leaked excessively from the fitting when the electric boost pump was turned on. After the fitting was tightened, the engine started without hesitation and ran continuously at idle power. Due to three bent propeller blades and vibration, a higher power setting was not attempted. A review of the airplane and engine logbooks found no entries indicating that any recent maintenance had been conducted on the fuel system.

Probable Cause: The improper installation of the fuel supply line fitting at the fuel manifold, which resulted in the line loosening in-flight, fuel leakage, and a subsequent total loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA15LA294
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB ERA15LA294

Location

Revision history:

Date/timeContributorUpdates
07-Oct-2022 06:49 ASN Update Bot Added

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