ASN Wikibase Occurrence # 290887
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 28 July 2015 |
Time: | 20:25 LT |
Type: | Eagle Aircraft Co EAGLE DW 1 |
Owner/operator: | |
Registration: | N8806B |
MSN: | DW-1-0039-81 |
Year of manufacture: | 1981 |
Total airframe hrs: | 2262 hours |
Engine model: | Lycoming IO-540-M1B5D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hector, Minnesota -
United States of America
|
Phase: | Approach |
Nature: | Agricultural |
Departure airport: | Hector, MN (1D6) |
Destination airport: | Hector, MN (1D6) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that new spray booms had been installed on the airplane and that he was returning to the airport after performing an aerial application test flight. During final approach for landing, the pilot noticed that the airplane was going to be short of the intended landing point, so he advanced the engine throttle to reestablish a proper glidepath. The engine did not respond as expected, so the pilot continued to advance the throttle; however, the engine still did not respond as expected. The pilot realized that the airplane was not going to reach the runway, so he applied maximum throttle, which resulted in the engine surging. He then increased the angle-of-attack in an attempt to gain maximum lift. However, the airplane's descent rate increased, and the spray booms subsequently contacted the bean field. The airplane then impacted the bean field, bounced, nosed over, and came to rest inverted. Postaccident examination of the engine did not reveal any mechanical malfunctions or failures that would have caused the intermittent partial power loss.
Probable Cause: The intermittent partial loss of engine power, which resulted in a lower-than-expected approach glidepath and impact with terrain short of the runway. The reason for the intermittent partial loss of engine power could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA326 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB CEN15LA326
Location
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 06:54 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation