ASN Wikibase Occurrence # 290918
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Date: | Thursday 16 July 2015 |
Time: | 14:15 LT |
Type: | Devoe CLIP WING |
Owner/operator: | |
Registration: | N80917 |
MSN: | 04-94-CW-0476 |
Year of manufacture: | 1994 |
Engine model: | Rotax 447 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Melbourne, Arkansas -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | MOUNTAIN HOME, AR (BPK |
Destination airport: | MELBOURNE, AR (42A) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The recreational pilot was delivering the airplane to a new owner at a nearby airport. During the delivery flight, the engine lost power. The pilot stated that the airplane was about 1,000 ft above the ground and that he thought the terrain looked suitable for a landing, so he did not deploy the parachute. However, as the airplane continued to descend, the pilot noted that the terrain was covered with tall grass but that, at the airplane's altitude, deploying the parachute was no longer an option. The airplane subsequently impacted rough terrain, and the pilot sustained serious injuries.
An examination of the wreckage revealed no preimpact flight control anomalies. Examination of the engine and propeller revealed no preimpact mechanical issues. The fuel filter and carburetor bowl contained some contamination and the temperature and dew point at the time of the accident were conducive to carburetor icing at glide and cruise power settings. In addition, the throttle was found in the "off" position. The investigation could not determine which of these conditions, if any, caused the loss of engine power.
Probable Cause: The loss of engine power for reasons that could not be determined based on the available evidence and the postaccident engine examination, which led to a forced landing on unsuitable terrain due to the pilot's decision not to deploy the ballistic parachute when sufficient altitude was available to do so.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA308 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB CEN15LA308
Location
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 07:13 |
ASN Update Bot |
Added |
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