ASN Wikibase Occurrence # 291512
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Date: | Sunday 17 January 2016 |
Time: | 18:35 LT |
Type: | Bellanca 17-30A |
Owner/operator: | |
Registration: | N194DW |
MSN: | 94-301021 |
Year of manufacture: | 1994 |
Total airframe hrs: | 565 hours |
Engine model: | Continental IO 520 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Overbrook, Oklahoma -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | McKinney, TX (T31) |
Destination airport: | McKinney, TX (T31) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot stated that he did not visually check the fuel level in the tanks before the personal cross-country flight but that he estimated that there was sufficient fuel on board for a 1-hour flight; the flight was expected to take 30 minutes. The pilot stated that, about 15 to 20 minutes into the flight, the engine started to surge, and it then experienced a total loss of power. The pilot's attempts to restart the engine were unsuccessful. He then attempted to circle to the north end of a nearby airport so he could land to the south instead of landing to the north with a light tailwind. While on final approach, the airplane contacted trees and terrain about 300 ft north of the runway end. A postaccident examination of the airplane revealed that the fuel system was intact. No fuel was found in the left wing tank, and 1/2 gallon of fuel was found in the right wing tank.
Probable Cause: The pilot's inadequate preflight fuel planning, which resulted in a total loss of engine power due to fuel exhaustion, and his subsequent decision to circle to the north end of the airport due to a light tailwind condition instead of making a downwind landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN16LA090 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB CEN16LA090
Location
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 14:49 |
ASN Update Bot |
Added |
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