ASN Wikibase Occurrence # 291696
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Date: | Sunday 22 October 2006 |
Time: | 06:41 LT |
Type: | Cessna 152 |
Owner/operator: | United Flight Services |
Registration: | N45929 |
MSN: | 15282946 |
Year of manufacture: | 1978 |
Total airframe hrs: | 11695 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Prunedale, California -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Watsonville Airport, CA (WVI/KWVI) |
Destination airport: | Salinas Municipal Airport, CA (SNS/KSNS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the flight instructor, he and his student departed on the flight when, about halfway to their destination, the engine cowling and instrument panel began to shake violently. He adjusted the mixture setting and scanned the instruments and noted that the engine oil temperature and pressure were still indicating in the normal range. Shortly after that, the engine began shaking and then stopped entirely and gray smoke filled the cockpit. The flight instructor noted flames coming from the nose area of the aircraft and attempted to find a suitable landing site through the smoke and haze. The flight instructor elected to land in an agricultural field. The airplane touched down on the main landing gear, and as the nose wheel touched down it dug into the dirt and the airplane nosed over. When the instructor and student exited the airplane, they again observed a small fire near the front engine area, but it extinguished itself. According to a Federal Aviation Administration (FAA) inspector, the engine was examined and a large hole was found on the bottom side of the engine crankcase between the number 1 and number 2 cylinders. A concentration of oil was found on the inside of the cowling at the same approximate location as the crankcase hole. FAA inspectors discovered that the number 1 connecting rod cap had separated from the connecting rod during engine operation. The reason for this occurrence is undetermined.
Probable Cause: Total loss of engine power due to failure of connecting rod cap during cruise flight for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX07LA016 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB LAX07LA016
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 17:50 |
ASN Update Bot |
Added |
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