ASN Wikibase Occurrence # 291700
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 21 October 2006 |
Time: | 10:50 LT |
Type: | Piper PA-38-112 |
Owner/operator: | |
Registration: | N2426N |
MSN: | 38-79A0837 |
Year of manufacture: | 1979 |
Total airframe hrs: | 7602 hours |
Engine model: | Lycoming O-235 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Wimberley, Texas -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | LAGO VISTA, TX (5R3) |
Destination airport: | Wimberley, TX |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The 201-hour private pilot departed at about 11:15 on a local cross-country flight with 6 quarts of oil in the engine and 12 gallons of fuel on board. After takeoff, he climbed to 2,500 with the electric boost pump on. Later, during cruise flight the "engine powered back" and the pilot tried to reapply full power to the engine by "checking the fuses and [fuel] primer, as well as, turning on the electric fuel pump and turning to the left fuel tank." The engine did not respond and the pilot elected to execute a forced landing in a field. During a telephone conversation with the NTSB IIC, the pilot stated that the engine "sputtered out" and "then came back, sputtering again" before "quitting completely." During the recovery of the airplane, recovery personnel reported draining 7 gallons of fuel from the right fuel tank and that the left tank was empty. An engine inspection was conducted on November 15, 2006. The engine sustained minimum impact damage during the accident sequence. The engine was rotated by hand; continuity through the engine's valve train and compression on each cylinder was established. The bracket air filter was in place, and appeared in good condition and free of obstructions. The airplane's electrical system was turned on and the electric fuel boost pump was switched on; the electric pump appeared to operate normally. Approximately two tablespoons of fuel was drained from the carburetor. The gascolator was opened and found to be dry and clear, the screen at the top of the gascolator was in-place and free of any debris. The engine was examined and no mechanical anomalies were noted. The airplane's information manual states under Fuel Limitations: "... The unusable fuel for this airplane has been determined as 1.0 gallon in each wing in critical flight attitudes." Additionally, the manual states that fuel consumption during cruise flight would be 6.5 gallons/hour (75%, Best Power setting).
Probable Cause: the pilot's inadequate pre-flight planning which resulted in fuel starvation and the subsequent the loss of engine power. A contributing factor was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW07LA009 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB DFW07LA009
Revision history:
Date/time | Contributor | Updates |
07-Oct-2022 17:56 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation