ASN Wikibase Occurrence # 292008
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Date: | Wednesday 26 July 2006 |
Time: | 07:45 LT |
Type: | Cessna 150J |
Owner/operator: | |
Registration: | N60816 |
MSN: | 15070596 |
Year of manufacture: | 1969 |
Total airframe hrs: | 7397 hours |
Engine model: | Continental O-200 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Napa, California -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Vacaville-Nut Tree Airport, CA (KVCB) |
Destination airport: | Napa County Airport, CA (APC/KAPC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane lost engine power and nosed over during a forced landing. The pilot performed a preflight inspection of the airplane and checked the fuel quantity in each wing tank using a fuel measuring stick. He reported that there was no fuel in the left fuel tank, and 5.5 gallons of usable fuel in the right fuel tank. The pilot stated that he had more than enough fuel for the expected 19-minute flight. He performed an engine run-up and executed a normal takeoff. After clearing the mountains west of the departure airport, he radioed the air traffic control tower at the destination airport and requested a special visual flight rules (SVFR) clearance for runway 18. The controller told the pilot to remain outside the class delta airspace and to expect a 10-minute delay for landing. The pilot remained outside the airspace by maneuvering in right circles over a landmark. The pilot said that at this point, the fuel in the right tank lost contact with the fuel pickup port and the engine lost power. The pilot could not make it to the airport from his location and chose to land in a field approximately 5 miles north of the airport. The pilot successfully landed in the field; however, when the nose wheel touched down it dug into the soil and the airplane nosed over. A Federal Aviation Administration inspector examined the airplane on scene and reported that he found no fuel in the left fuel tank and no more than 6 gallons of fuel in the right fuel tank.
Probable Cause: a loss of engine power due to fuel starvation. The fuel starvation was the result of the pilot's inadequate preflight preparation (failure to refuel the airplane before taking off) and his inadequate in-flight decision (to make right turns while holding) that directly led to an unporting of the right fuel tank.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX06CA245 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB LAX06CA245
Revision history:
Date/time | Contributor | Updates |
08-Oct-2022 13:23 |
ASN Update Bot |
Added |
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