ASN Wikibase Occurrence # 292331
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Date: | Wednesday 17 May 2006 |
Time: | 13:00 LT |
Type: | Cessna 152 |
Owner/operator: | Skinner Aviation, Inc |
Registration: | N69183 |
MSN: | 15282533 |
Year of manufacture: | 1978 |
Engine model: | Lycoming O-235 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Klamath Falls, Oregon -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Plush, OR |
Destination airport: | Ashland, OR (S03) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:In a telephone conversation and subsequent written statement, the pilot reported that during the return leg to Ashland, he become disoriented and requested vectors to the nearest airport because of concerns about the aircraft's total time aloft and "...my fuel situation." Seattle Center advised the pilot that Chiloquin, Oregon, was approximately 10 miles north-northwest of his position, however it was not known if fuel was available at the airport and the ATC Specialist asked the pilot if Klamath Falls, approximately 35 miles from his location, would be an option. The pilot believed he had sufficient fuel to complete the flight to Klamath, however approximately 2 miles from reaching the airport the airplane's engine began to surge and eventually lost power. The pilot stated that he was unable to reach the runway and elected to land in an open field. As the airplane touched down in the field, it encountered soft muddy terrain and "flipped nose over." The pilot reported that he believed he had approximately 15 minutes of fuel remaining when the airplane lost engine power, however he later stated the airplane "just ran out of fuel." The airplane was "topped" prior to departing Ashland. The Hobbs meter indicated that the airplane had flown approximately 3.6 hours since it had been fueled.
Probable Cause: The pilot's inadequate in-flight decision by failing to refuel while en route, resulting in fuel exhaustion and the loss of engine power. Soft terrain was a contributing factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA06CA099 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB SEA06CA099
Revision history:
Date/time | Contributor | Updates |
08-Oct-2022 17:26 |
ASN Update Bot |
Added |
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