Accident Eurocopter AS 350B3 N183AE,
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ASN Wikibase Occurrence # 292333
 
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Date:Tuesday 16 May 2006
Time:09:10 LT
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Eurocopter AS 350B3
Owner/operator:U.S. Department Of Homeland Security
Registration: N183AE
MSN: 3852
Year of manufacture:2005
Total airframe hrs:352 hours
Engine model:Turbomeca ARRIEL 2B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Santa Teresa, NM -   United States of America
Phase: Unknown
Nature:Training
Departure airport:Santa Teresa, NM
Destination airport:El Paso International Airport, TX (ELP/KELP)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The purpose of the instructional flight was to conduct simulated emergency governor operations. The single-engine helicopter landed hard in a near level flight attitude in a slight tail low attitude. The landing gear skids collapsed on impact causing the lower vertical fin and tail rotor assembly to make contact with the ground, bucking the tailboom at the forward attaching points. The helicopter slid on it's fuselage 250 feet from the point of impact and came to rest in an upright position. The left pilot seat attenuated as designed but there was no evidence of attenuation on the right pilot seat. The crew performed an emergency engine shutdown and egressed unassisted. The wreckage of the helicopter was recovered to the facilities of the operator's secured facilities for further examination. The investigator examined the helicopter systems and tested the throttle twist grip for anomalies. The tests on the throttle twist grip simulated actions taken during the training flight. Several cycles of the governor from the "auto" mode to the "manual" mode for two minutes and back to the auto made for 3 minutes were performed to determine if a problem would occur that would restrict manual throttle operation. The examination determined after several cycles, that the solenoid that retracted to allow manual throttle manipulation would not fully retract and created a restriction due to heat generated during the activation. The helicopter seats were examined to determine if the any anomalies existed with the crash attenuating seats. The left front seat was documented as fully attenuating during the crash sequence and the right front seat had not attenuated. The seats were shipped for analysis to it's manufacturer's facilities in France for further testing. The examination and testing revealed that the seats met specifications and evidence on the right seat showed that the seat attenuation was initiating but did not appear to have sustained sufficient forces to fully stroke.

Probable Cause: The flight instructor's improper supervision of the flight which resulted in a hard landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DFW06TA127
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB DFW06TA127

Revision history:

Date/timeContributorUpdates
08-Oct-2022 17:27 ASN Update Bot Added
01-Jun-2023 11:21 Ron Averes Updated

Corrections or additions? ... Edit this accident description

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