Fuel exhaustion Accident Cessna TR182 N729SC,
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ASN Wikibase Occurrence # 292466
 
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Date:Tuesday 11 April 2006
Time:12:30 LT
Type:Silhouette image of generic C82R model; specific model in this crash may look slightly different    
Cessna TR182
Owner/operator:Charles Ksir
Registration: N729SC
MSN: R18200750
Total airframe hrs:3954 hours
Engine model:Lycoming O-540-L3C5D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Fort Collins, Colorado -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Carlsbad Airport, NM (CNM/KCNM)
Destination airport:Laramie Regional Airport, WY (LAR/KLAR)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Prior to departure, the pilot estimated the airplane's fuel tanks contained approximately 70 gallons of fuel, and he planned a usage of 50 gallons for flight. While in cruise flight at 10,500 feet, the pilot encountered light and occasional moderate turbulence. Because of the turbulence, the pilot reduced the engine power several times to slow the aircraft. At least three times during the flight, the pilot lowered the landing gear to slow the aircraft and to increase stability. While en route at an altitude of 8,500 feet, the engine lost power. The pilot noticed on the fuel gauges that the right tank appeared empty and the left tank indicated more than 1/4 tank of fuel. The pilot switched the fuel selector to the left tank and the engine regained power. The pilot then decided to land at a nearby airport to add some fuel, check the magnetos and ground run the engine before continuing to his intended destination. Approximately 9 miles from the airport, the pilot lowered the landing gear and initiated a descent to the airport's pattern altitude. During the descent, the engine "faltered and surged" 4 to 5 times. The pilot then trimmed the airplane for a 60 knot glide speed, declared an emergency on UNICOM frequency and attempted a landing to the nearest runway. Shortly thereafter, the engine lost power, and the pilot initiated a forced landing to a field. During the forced landing, the airplane contacted a fence and a berm, and the nose gear collapsed, buckling the firewall. According to the recovery personnel, less than 1 gallon of fuel was recovered from the wing tanks and airframe fuel lines. The fuel sending units were removed from the wings and functionally tested. A functional check of the sending units and cockpit fuel gauges revealed no anomalies.


Probable Cause: the loss of engine power due to fuel exhaustion. Contributing factors were the pilot's improper preflight planning, the pilot's failure to refuel the airplane, and the lack of suitable terrain for the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN06LA059
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB DEN06LA059

Revision history:

Date/timeContributorUpdates
08-Oct-2022 19:00 ASN Update Bot Added

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