ASN Wikibase Occurrence # 292522
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 29 March 2006 |
Time: | 08:40 LT |
Type: | Piper PA-28-180 |
Owner/operator: | Private |
Registration: | N2182T |
MSN: | 28-7205037 |
Total airframe hrs: | 5812 hours |
Engine model: | Lycoming O-360-A4A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bunnell, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Bunnell, FL (X47) |
Destination airport: | Ormond Beach Municipal Airport, FL (KOMN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that earlier that morning he flew to the Flagler County Airport, landed, and secured the engine. He then elected to return to the departure airport. He did not perform a preflight inspection of the airplane, and after starting the engine he taxied to and departed from runway 29. During the initial climb at approximately 1,500 feet he noted smoke coming from the engine compartment and the engine experienced a partial loss of power. He turned to return to the airport and the engine seized. He performed a forced landing on a dirt road and during the landing roll ran off the road and collided with a tree. Post accident examination of the engine by an FAA airworthiness inspector revealed an oil film inside the engine cowling and also on the right side of the fuselage from the engine cowling to midspan of the right wing. Additionally, damage to one of the cylinders was noted. The engine driven vacuum pump was found to have not been installed correctly with incorrect gasket material which was baffle gasket material and that the nuts that hold and seal the vacuum pump on were not torqued to proper specs and/or were missing all together and that there was oil on the rubber gaskets. The owner/pilot admitted to having worked along side with the IA to install the engine driven vacuum pump. The owner/pilot also stated that after they were finished installing the pump, he asked the IA if they had installed it correctly because it was sticking out more then he was used to. The IA reported having supervised the owner/pilot who did the work, then checked what he had done and signed it off. The engine had only 8 hours and was within a month of being overhauled at the time of the accident.
Probable Cause: The failure of the pilot to perform a preflight inspection of the airplane resulting in departure with an inadequate oil supply, subsequent engine failure due to oil starvation, and damage to the airplane during a forced landing. Contributing to the accident was the improper installation of the engine-driven vacuum pump by a mechanic.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA06LA073 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB MIA06LA073
Revision history:
Date/time | Contributor | Updates |
08-Oct-2022 19:41 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation