ASN Wikibase Occurrence # 292570
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 12 March 2006 |
Time: | 15:00 LT |
Type: | Sessi Midget Mustang SK-1 |
Owner/operator: | Private |
Registration: | N202 |
MSN: | 501 |
Total airframe hrs: | 1198 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Everett, Washington -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Everett-Snohomish County Airport, WA (PAE/KPAE) |
Destination airport: | Caldwell Industrial Airport, ID (KEUL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he just purchased this aircraft and this was his first flight in the aircraft to fly it back home to Texas. The pilot stated that during the takeoff roll from runway 34 left, the engine was running smooth. Full throttle was applied and at approximately 70 mph, lift off occurred and the aircraft entered a nose high attitude and began a continuous stall buffet. The pilot pitched the nose down to gain airspeed several times. Each time he pulled the stick back it would stall. The pilot stated that the aircraft attained about 30 to 35 feet above ground level, and while he was scanning the engine instruments, the aircraft drifted to the left of the runway. The pilot applied "hard right aileron to avoid hitting glide slope antenna..." The aircraft stalled and impacted the terrain next to the runway in an uncontrolled attitude with full throttle. The pilot stated that this was also the first flight for this aircraft since a new wood propeller had been put on, after an earlier event prior to the purchase, in which the original propeller had been damaged. The pilot indicated that the wrong pitch and diameter propeller had been used and the aircraft was signed off as airworthy without having been test flown. The propeller blades were destroyed during the crash sequence.
Probable Cause: The pilot did not abort the takeoff and subsequently did not maintain aircraft control during the initial takeoff climb. The installation of the wrong propeller assembly and inadequate maintenance were factors.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA06LA064 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB SEA06LA064
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 06:15 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation